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For Mega/Mix enabled SoCs like MX7D and MX6SX, uSDHC will lost power in
LP mode no matter whether the MMC_KEEP_POWER flag is set or not.
This may cause state misalign between kernel and HW, especially for
SDIO3.0 WiFi cards.
e.g. SDIO WiFi driver usually will keep power during system suspend.
And after resume, no card re-enumeration called.
But the tuning state is lost due to Mega/Mix.
Then CRC error may happen during next data transfer.
So we should always fire a mmc_retune_needed() for such type SoC
to tell MMC core retuning is needed for next data transfer.
mmc: sdhci-esdhci-imx: retune needed for Mega/Mix enabled SoCs
Signed-off-by: Haibo Chen <haibo.chen@nxp.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/1582100563-20555-4-git-send-email-haibo.chen@nxp.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
When using jailhouse to support two Linux on i.MX8MQ EVK, we use the
1st Linux to configure pinctrl for the 2nd Linux. Then the 2nd Linux
could use the mmc without pinctrl driver.
So give a warning message when no pinctrl available, but no fail probe.
Signed-off-by: Haibo Chen <haibo.chen@nxp.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Acked-by: Linus Walleij <linus.walleij@linaro.org>
Link: https://lore.kernel.org/r/1582100563-20555-3-git-send-email-haibo.chen@nxp.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Except SDHCI_QUIRK_BROKEN_CARD_DETECTION and MMC_CAP_NONREMOVABLE,
we also do not need to handle controller native card detect interrupt
for gpio cd type.
If we wrong enabled the card detect interrupt for gpio case, it will
cause a lot of unexpected card detect interrupts during data transfer
which should not happen.
Signed-off-by: Haibo Chen <haibo.chen@nxp.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Link: https://lore.kernel.org/r/1582100563-20555-2-git-send-email-haibo.chen@nxp.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Its recommended that DLL must only be enabled for SDR50, DDR50, DDR52,
SDR104, HS200 and HS400 speed modes. Move DLL configuration to its own
function and call it only in the above speed modes.
Signed-off-by: Faiz Abbas <faiz_abbas@ti.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/20200108150920.14547-4-faiz_abbas@ti.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
According to the latest AM65x Data Manual[1], a different output tap
delay value is optimum for a given speed mode. Therefore, deprecate the
ti,otap-del-sel binding and introduce a new binding for each of the
possible MMC/SD speed modes. If the legacy mode is not found, fall back
to old binding to maintain dts compatibility.
[1] http://www.ti.com/lit/gpn/am6526
Signed-off-by: Faiz Abbas <faiz_abbas@ti.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/20200108150920.14547-3-faiz_abbas@ti.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Add missing MODULE_LICENSE() and MODULE_DESCRIPTION() in hsq driver to
fix below warning when compiling the hsq as a module.
"WARNING: modpost: missing MODULE_LICENSE() in drivers/mmc/host/mmc_hsq.o".
Reported-by: Stephen Rothwell <sfr@canb.auug.org.au>
Signed-off-by: Baolin Wang <baolin.wang7@gmail.com>
Link: https://lore.kernel.org/r/98ce471185f037fce57520763621590588766381.1582161803.git.baolin.wang7@gmail.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This patch adds a sdmmc variant revision 2.0. This revision is backward
compatible with 1.1, but adds DMA linked list support.
Signed-off-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200128090636.13689-10-ludovic.barre@st.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
To prepare the voltage switch procedure, the VSWITCHEN bit must be set
before sending the CMD11. To confirm completion of voltage switch, the
VSWEND flag must be checked.
Signed-off-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200128090636.13689-9-ludovic.barre@st.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
A variant may need to define some actions before and after a voltage
switch.
This patch adds 2 callbacks to manage signal voltage switch in the struct
mmci_host_ops. ->pre_sig_volt_switch() allows to prepare a signal voltage
switch before sending the SD_SWITCH_VOLTAGE command (CMD11).
->post_sig_volt_switch callback allows specific actions to be executed,
after the I/O signal voltage level has been changed.
Signed-off-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200128090636.13689-8-ludovic.barre@st.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The hardware delay block is used to align the sampling clock on the data
received by SDMMC. It is mandatory for SDMMC to support the SDR104 mode.
The delay block is used to generate an output clock which is dephased from
the input clock. The phase of the output clock must be programmed by the
execute tuning interface.
Signed-off-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200128090636.13689-7-ludovic.barre@st.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In variant init function, some references may be allocated for variant
specific usage. Add a private void* to mmci_host struct allows at variant
functions to access on this references by mmci_host structure.
Signed-off-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200128090636.13689-5-ludovic.barre@st.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The variant init function may need to add a mmc_host_ops, for example to
add the execute_tuning support if this feature is available. This patch
adds mmc_host_ops pointer in mmci struct.
Signed-off-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200128090636.13689-4-ludovic.barre@st.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
sg_dma_xxx should be used after a dma_map_sg call has been done to get bus
addresses of each of the SG entries and their lengths. But mmci_host_ops
validate_data can be called before dma_map_sg. This patch replaces theses
macros by sg->offset and sg->length which are always defined.
Signed-off-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200128090636.13689-2-ludovic.barre@st.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In case the host specify a max_busy_timeout, we need to validate that the
needed timeout for the HPI command conforms to that requirement. If that's
not the case, let's convert from a R1B response to a R1 response, as to
instruct the host to avoid HW busy detection.
Additionally, when R1B is used we must also inform the host about the busy
timeout for the command, so let's do that via updating cmd.busy_timeout.
Finally, when R1B is used and in case the host supports HW busy detection,
there should be no need for doing polling, so then skip that.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Tested-by: Ludovic Barre <ludovic.barre@st.com>
Reviewed-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200204085449.32585-12-ulf.hansson@linaro.org
Rather than open coding the polling loop in mmc_interrupt_hpi(), let's
convert to use mmc_poll_for_busy().
Note that, moving to mmc_poll_for_busy() for HPI also improves the
behaviour according to below.
- Adds support for polling via the optional ->card_busy() host ops.
- Require R1_READY_FOR_DATA to be set in the CMD13 response before exiting
the polling loop.
- Adds a throttling mechanism to avoid CPU hogging when polling.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Tested-by: Ludovic Barre <ludovic.barre@st.com>
Reviewed-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200204085449.32585-11-ulf.hansson@linaro.org
The 'u32 *status' is unused by the caller, so let's drop it.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Tested-by: Ludovic Barre <ludovic.barre@st.com>
Reviewed-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200204085449.32585-10-ulf.hansson@linaro.org
Rather than open coding the polling loop in mmc_do_erase(), let's convert
to use mmc_poll_for_busy().
To allow a slightly different error parsing during polling, compared to the
__mmc_switch() case, a new in-parameter to mmc_poll_for_busy() is needed,
but other than that the conversion is straight forward.
Besides addressing the open coding issue, moving to mmc_poll_for_busy() for
erase/trim/discard improves the behaviour according to below.
- Adds support for polling via the optional ->card_busy() host ops.
- Returns zero to indicate success when the final polling attempt finds the
card non-busy, even if the timeout expired.
- Exits the polling loop when state moves to R1_STATE_TRAN, rather than
when leaving R1_STATE_PRG.
- Decreases the starting range for throttling to 32-64us.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Tested-by: Ludovic Barre <ludovic.barre@st.com>
Reviewed-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200204085449.32585-9-ulf.hansson@linaro.org
Through mmc_poll_for_busy() a CMD13 may be sent to get the status of the
(e)MMC card. If the state of the card is R1_STATE_PRG, the card is
considered as being busy, which means we continue to poll with CMD13. This
seems to be sufficient, but it's also unnecessary fragile, as it means a
new command/request could potentially be sent to the card when it's in an
unknown state.
To try to improve the situation, but also to move towards a more consistent
CMD13 polling behaviour in the mmc core, let's deploy the same policy we
use for regular I/O write requests. In other words, let's check that card
returns to the R1_STATE_TRAN and that the R1_READY_FOR_DATA bit is set in
the CMD13 response, before exiting the polling loop.
Note that, potentially this changed behaviour could lead to unnecessary
waiting for the timeout to expire, if the card for some reason, moves to an
unexpected error state. However, as we bail out from the polling loop when
R1_SWITCH_ERROR bit is set or when the CMD13 fails, this shouldn't be an
issue.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Tested-by: Ludovic Barre <ludovic.barre@st.com>
Reviewed-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200204085449.32585-8-ulf.hansson@linaro.org
To allow subsequent changes to re-use the code from the static function
mmc_blk_in_tran_state(), let's move it to a public header. While at it,
let's also rename it to mmc_ready_for_data(), as to try to better describe
its purpose.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Tested-by: Ludovic Barre <ludovic.barre@st.com>
Reviewed-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200204085449.32585-7-ulf.hansson@linaro.org
To make the code more readable, move the part that gets the busy status of
the card out into a separate function, mmc_busy_status(). Then call it from
mmc_poll_for_busy().
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Tested-by: Ludovic Barre <ludovic.barre@st.com>
Reviewed-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200204085449.32585-6-ulf.hansson@linaro.org
The use_busy_signal in-parameter is set true by all callers of
__mmc_switch(), hence it's redundant so drop it.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Tested-by: Ludovic Barre <ludovic.barre@st.com>
Reviewed-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200204085449.32585-5-ulf.hansson@linaro.org
To simplify code, let's extend mmc_switch_status() to cope with needs
addressed in __mmc_switch_status(). Then move all users to the updated
mmc_switch_status() API and drop __mmc_switch_status() altogether.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Tested-by: Ludovic Barre <ludovic.barre@st.com>
Reviewed-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200204085449.32585-4-ulf.hansson@linaro.org
The last user of MMC_OPS_TIMEOUT_MS was recently removed, however the
define stayed around. Let's remove it.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Tested-by: Ludovic Barre <ludovic.barre@st.com>
Reviewed-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200204085449.32585-3-ulf.hansson@linaro.org
In mmc_poll_for_busy() we loop continuously, either by sending a CMD13 or
by invoking the ->card_busy() host ops, as to detect when the card stops
signaling busy. This behaviour is problematic as it may cause CPU hogging,
especially when the busy signal time reaches beyond a few ms.
Let's fix the issue by adding a throttling mechanism, that inserts a
usleep_range() in between the polling attempts. The sleep range starts at
32-64us, but increases for each loop by a factor of 2, up until the range
reaches ~32-64ms. In this way, we are able to keep the loop fine-grained
enough for short busy signaling times, while also not hogging the CPU for
longer times.
Note that, this change is inspired by the similar throttling mechanism that
we already use for mmc_do_erase().
Reported-by: Michał Mirosław <mirq-linux@rere.qmqm.pl>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Baolin Wang <baolin.wang7@gmail.com>
Tested-by: Ludovic Barre <ludovic.barre@st.com>
Reviewed-by: Ludovic Barre <ludovic.barre@st.com>
Link: https://lore.kernel.org/r/20200204085449.32585-2-ulf.hansson@linaro.org
When using the host software queue, it will trigger the next request in
irq handler without a context switch. But the sdhci_request() can not be
called in interrupt context when using host software queue for some host
drivers, due to the get_cd() ops can be sleepable.
But for some host drivers, such as Spreadtrum host driver, the card is
nonremovable, so the get_cd() ops is not sleepable, which means we can
complete the data request and trigger the next request in irq handler
to remove the context switch for the Spreadtrum host driver.
As suggested by Adrian, we should introduce a request_atomic() API to
indicate that a request can be called in interrupt context to remove
the context switch when using mmc host software queue. But this should
be done in another thread to convert the users of mmc host software queue.
Thus we can introduce a variable in struct sdhci_host to indicate that
we will always to defer to complete requests when using the host software
queue.
Suggested-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Baolin Wang <baolin.wang@linaro.org>
Signed-off-by: Baolin Wang <baolin.wang7@gmail.com>
Link: https://lore.kernel.org/r/e693e7a29beb3c1922b333f4603ea81f43d5c5b1.1581478568.git.baolin.wang7@gmail.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Add request_done ops for struct sdhci_ops as a preparation in case some
host controllers have different method to complete one request, such as
supporting request completion of MMC software queue.
Suggested-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Baolin Wang <baolin.wang@linaro.org>
Signed-off-by: Baolin Wang <baolin.wang7@gmail.com>
Link: https://lore.kernel.org/r/1539c801c8bbdbcd1d86f8c2dab375f5803c765a.1581478568.git.baolin.wang7@gmail.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Enable the MMC host software queue for the SD card if the host controller
supports the MMC host software queue.
On my Spreadtrum platform, I did not see any obvious performance changes
in 4K block size when changing to use hsq for the SD cards, I think the
reason is the SD card works at a low speed on my platform, and most of
time is spent in the hardware. But we can see some obvious improvements
when enabling the packed request based on hsq, that's why we still add hsq
support for the SD cards.
Signed-off-by: Baolin Wang <baolin.wang@linaro.org>
Signed-off-by: Baolin Wang <baolin.wang7@gmail.com>
Link: https://lore.kernel.org/r/0065b4631fef2d61c3b89d14a4ea4f2b7499ea56.1581478568.git.baolin.wang7@gmail.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Now the MMC read/write stack will always wait for previous request is
completed by mmc_blk_rw_wait(), before sending a new request to hardware,
or queue a work to complete request, that will bring context switching
overhead and spend some extra time to poll the card for busy completion
for I/O writes via sending CMD13, especially for high I/O per second
rates, to affect the IO performance.
Thus this patch introduces MMC software queue interface based on the
hardware command queue engine's interfaces, which is similar with the
hardware command queue engine's idea, that can remove the context
switching. Moreover we set the default queue depth as 64 for software
queue, which allows more requests to be prepared, merged and inserted
into IO scheduler to improve performance, but we only allow 2 requests
in flight, that is enough to let the irq handler always trigger the
next request without a context switch, as well as avoiding a long latency.
Moreover the host controller should support HW busy detection for I/O
operations when enabling the host software queue. That means, the host
controller must not complete a data transfer request, until after the
card stops signals busy.
From the fio testing data in cover letter, we can see the software
queue can improve some performance with 4K block size, increasing
about 16% for random read, increasing about 90% for random write,
though no obvious improvement for sequential read and write.
Moreover we can expand the software queue interface to support MMC
packed request or packed command in future.
Reviewed-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: Baolin Wang <baolin.wang@linaro.org>
Signed-off-by: Baolin Wang <baolin.wang7@gmail.com>
Link: https://lore.kernel.org/r/4409c1586a9b3ed20d57ad2faf6c262fc3ccb6e2.1581478568.git.baolin.wang7@gmail.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
SDHC core with new 14lpp and later tech DLL should not enable
PWRSAVE_DLL since such controller's internal gating cannot meet
following MCLK requirement:
When MCLK is gated OFF, it is not gated for less than 0.5us and MCLK
must be switched on for at-least 1us before DATA starts coming.
Adding support for this requirement.
Signed-off-by: Ritesh Harjani <riteshh@codeaurora.org>
Signed-off-by: Veerabhadrarao Badiganti <vbadigan@codeaurora.org>
Reviewed-by: Can Guo <cang@codeaurora.org>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/1581077075-26011-1-git-send-email-vbadigan@codeaurora.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This patch removes quirk which indicates a broken base clock. This was
making the kernel report wrong base clock of ~187MHz instead of 200MHz
even as the measurement on the hardware was showing 200MHz.
Signed-off-by: Manish Narani <manish.narani@xilinx.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/1579602095-30060-5-git-send-email-manish.narani@xilinx.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The DLL resets are required while executing the auto tuning procedure in
ZynqMP. This patch adds code to support the same.
Signed-off-by: Manish Narani <manish.narani@xilinx.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/1579602095-30060-4-git-send-email-manish.narani@xilinx.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
After various refactoring, we can populate the mmc_ops callbacks
directly and don't need to have wrappers for them anymore.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Niklas Söderlund <niklas.soderlund+renesas@ragnatech.se>
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Link: https://lore.kernel.org/r/20200129203709.30493-7-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
TAPs are Renesas SDHI specific. Now that we moved all handling to the
SDHI core, we can also move the definitions from the TMIO struct to the
SDHI one.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Niklas Söderlund <niklas.soderlund+renesas@ragnatech.se>
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Link: https://lore.kernel.org/r/20200129203709.30493-6-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Currently, select_tuning() is called after RPM resume. But
select_tuning() needs some additional function calls to work correctly.
Instead of reimplementing the whole postprocessing, just enforce
retuning.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Link: https://lore.kernel.org/r/20200129203709.30493-5-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
check_scc_error() is too Renesas specific. Let's just call it
check_retune() to make it also easier understandable what it does.
Only a rename, no functional change.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Niklas Söderlund <niklas.soderlund+renesas@ragnatech.se>
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Link: https://lore.kernel.org/r/20200129203709.30493-4-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
When the tap array in the driver is too low, this is not a warning but
an error. Also _once is not helpful, we should make sure it is
prominently in the logs. It is safe to do this because this will only
show up during SoC enablement when we a new SoCs needs more taps (if
that ever will happen).
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Niklas Söderlund <niklas.soderlund+renesas@ragnatech.se>
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Link: https://lore.kernel.org/r/20200129203709.30493-3-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Move Renesas specific code for executing the tuning with a SCC into the
SDHI driver and leave only a generic call in the TMIO driver. Simplify
the code a little by removing init_tuning() and prepare_tuning()
callbacks. The latter is directly folded into the new execute_tuning()
callbacks.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Niklas Söderlund <niklas.soderlund+renesas@ragnatech.se>
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Link: https://lore.kernel.org/r/20200129203709.30493-2-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Use increasing BIT numbers consistently and remove some superfluous
comments.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Link: https://lore.kernel.org/r/20191217114034.13290-6-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
HW engineers say that automatic tap correction cannot be used for HS400
in all R-Car Gen3 SoCs. So, check for that SDHI variant and disable it
when HS400 is about to be enabled.
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Link: https://lore.kernel.org/r/20191217114034.13290-5-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
R-Car Gen3 cannot use correction error status with HS400.
HS200: CMD and DAT signal timing are based on CLK signal.
HS400: CMD signal is based on CLK. DAT signal is based on DS signal.
In HS400, CMD signal is 200MHz(SDR). DAT signal is 200MHz(DDR).
Center position of signal is different between CMD and DAT.
TAP position should be adjusted to the center position of CMD signal.
DAT sampling timing is adjusted by HS400 calibration circuit regardless
of TAP position. Refer to renesas_sdhi_adjust_hs400mode_enable().
However, correction error status contains CMD and DAT status in HS400
(DAT signal is not masked in HS400). Therefore, correction error status
cannot use in HS400. It means that auto correction cannot be uses in
HS400. Manual correction can change to the correct TAP position by
ignoring DAT correction error status and using only CMD correction
status.
Signed-off-by: Takeshi Saito <takeshi.saito.xv@renesas.com>
[wsa: refactored patch from BSP]
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Link: https://lore.kernel.org/r/20191217114034.13290-4-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This patch adds a manual correction mechanism for SDHI. Currently, SDHI
uses automatic TAP position correction. However, TAP position can also
be corrected manually via correction error status flags.
Signed-off-by: Takeshi Saito <takeshi.saito.xv@renesas.com>
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Link: https://lore.kernel.org/r/20191217114034.13290-3-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
hw_reset() clears the automatic correction bit twice. I couldn't find
anything in the docs recommending that. Removing one of them didn't
cause any regressions here, so keep it simple.
Reviewed-by: Yoshihiro Shimoda <yoshihiro.shimoda.uh@renesas.com>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Link: https://lore.kernel.org/r/20191217114034.13290-2-wsa+renesas@sang-engineering.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The TX/RX register should not be treated the same way to allow for better
support of tuning. Fix this by using a default initial value for TX.
Signed-off-by: Ricky Wu <ricky_wu@realtek.com>
Cc: stable@vger.kernel.org
Link: https://lore.kernel.org/r/20200316025232.1167-1-ricky_wu@realtek.com
[Ulf: Updated changelog]
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
SAMA5D2x doesn't drive CMD line if GPIO is used as CD line (at least
SAMA5D27 doesn't). Fix this by forcing card-detect in the module
if module-controlled CD is not used.
Fixed commit addresses the problem only for non-removable cards. This
amends it to also cover gpio-cd case.
Cc: stable@vger.kernel.org
Fixes: 7a1e3f1431 ("mmc: sdhci-of-at91: force card detect value for non removable devices")
Signed-off-by: Michał Mirosław <mirq-linux@rere.qmqm.pl>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Link: https://lore.kernel.org/r/8d10950d9940468577daef4772b82a071b204716.1584290561.git.mirq-linux@rere.qmqm.pl
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The SDHCI_PRESET_FOR_* registers are not set for the UniPhier platform
integration. (They are all read as zeros).
Set the SDHCI_QUIRK2_PRESET_VALUE_BROKEN quirk flag. Otherwise, the
High Speed DDR mode on the eMMC controller (MMC_TIMING_MMC_DDR52)
would not work.
I split the platform data to give no impact to other platforms,
although the UniPhier platform is currently only the upstream user
of this IP.
The SDHCI_QUIRK2_PRESET_VALUE_BROKEN flag is set if the compatible
string matches to "socionext,uniphier-sd4hc".
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Cc: stable@vger.kernel.org
Link: https://lore.kernel.org/r/20200312104257.21017-1-yamada.masahiro@socionext.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
On the Acer Aspire Switch 10 (SW5-012) microSD slot always reports the card
being write-protected even though microSD cards do not have a write-protect
switch at all.
Add a new DMI_QUIRK_SD_NO_WRITE_PROTECT quirk which when set sets
the MMC_CAP2_NO_WRITE_PROTECT flag on the controller for the external SD
slot; and add a DMI quirk table entry which selects this quirk for the
Acer SW5-012.
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Cc: stable@vger.kernel.org
Link: https://lore.kernel.org/r/20200316184753.393458-2-hdegoede@redhat.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Based on a sample of 7 DSDTs from Cherry Trail devices using an AXP288
PMIC depending on the design one of 2 possible LDOs on the PMIC is used
for the MMC signalling voltage, either DLDO3 or GPIO1LDO (GPIO1 pin in
low noise LDO mode).
The Lenovo Miix 320-10ICR uses GPIO1LDO in the SHC1 ACPI device's DSM
methods to set 3.3 or 1.8 signalling voltage and this appears to work
as advertised, so presumably the device is actually using GPIO1LDO for
the external microSD signalling voltage.
But this device has a bug in the _PS0 method of the SHC1 ACPI device,
the DSM remembers the last set signalling voltage and the _PS0 restores
this after a (runtime) suspend-resume cycle, but it "restores" the voltage
on DLDO3 instead of setting it on GPIO1LDO as the DSM method does. DLDO3
is used for the LCD and setting it to 1.8V causes the LCD to go black.
This commit works around this issue by calling the Intel DSM to reset the
signal voltage to 3.3V after the host has been runtime suspended.
This will make the _PS0 method reprogram the DLDO3 voltage to 3.3V, which
leaves it at its original setting fixing the LCD going black.
This commit adds and uses a DMI quirk mechanism to only trigger this
workaround on the Lenovo Miix 320 while leaving the behavior of the
driver unchanged on other devices.
BugLink: https://bugs.freedesktop.org/show_bug.cgi?id=111294
BugLink: https://gitlab.freedesktop.org/drm/intel/issues/355
Reported-by: russianneuromancer <russianneuromancer@ya.ru>
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Cc: stable@vger.kernel.org
Link: https://lore.kernel.org/r/20200316184753.393458-1-hdegoede@redhat.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The busy timeout for the CMD5 to put the eMMC into sleep state, is specific
to the card. Potentially the timeout may exceed the host->max_busy_timeout.
If that becomes the case, mmc_sleep() converts from using an R1B response
to an R1 response, as to prevent the host from doing HW busy detection.
However, it has turned out that some hosts requires an R1B response no
matter what, so let's respect that via checking MMC_CAP_NEED_RSP_BUSY. Note
that, if the R1B gets enforced, the host becomes fully responsible of
managing the needed busy timeout, in one way or the other.
Suggested-by: Sowjanya Komatineni <skomatineni@nvidia.com>
Cc: <stable@vger.kernel.org>
Link: https://lore.kernel.org/r/20200311092036.16084-1-ulf.hansson@linaro.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>