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Convert platform_get_resource(), devm_ioremap_resource() to a single
call to devm_platform_get_and_ioremap_resource(), as this is exactly
what this function does.
Signed-off-by: Yangtao Li <frank.li@vivo.com>
Link: https://lore.kernel.org/r/20230712062853.11007-14-frank.li@vivo.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The DT of_device.h and of_platform.h date back to the separate
of_platform_bus_type before it as merged into the regular platform bus.
As part of that merge prepping Arm DT support 13 years ago, they
"temporarily" include each other. They also include platform_device.h
and of.h. As a result, there's a pretty much random mix of those include
files used throughout the tree. In order to detangle these headers and
replace the implicit includes with struct declarations, users need to
explicitly include the correct includes.
Signed-off-by: Rob Herring <robh@kernel.org>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de> # for imx
Link: https://lore.kernel.org/r/20230724205440.767071-1-robh@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Since commit 79d0224f6bf2 ("tty: serial: imx: Handle RS485 DE signal
active high") RS485 reception no longer works after a transmission.
The following scenario shows the problem:
1) Open a port in RS485 mode
2) Receive data from remote (OK)
3) Transmit data to remote (OK)
4) Receive data from remote (Nothing received)
In RS485 mode, imx_uart_start_tx() calls imx_uart_stop_rx() and, when the
transmission is complete, imx_uart_stop_tx() calls imx_uart_start_rx().
Since the above commit imx_uart_stop_rx() now sets the loopback bit but
imx_uart_start_rx() does not clear it causing the hardware to remain in
loopback mode and not receive external data.
Fix this by moving the existing loopback disable code to a helper function
and calling it from imx_uart_start_rx() too.
Fixes: 79d0224f6bf2 ("tty: serial: imx: Handle RS485 DE signal active high")
Cc: stable@vger.kernel.org
Signed-off-by: Martin Fuzzey <martin.fuzzey@flowbird.group>
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20230616104838.2729694-1-martin.fuzzey@flowbird.group
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The return value is only ever used as a return value for remove callbacks
of platform drivers. This return value is ignored by the driver core.
(The only effect is an error message, but uart_remove_one_port() already
emitted one in this case.)
So the return value isn't used at all and uart_remove_one_port() can be
changed to return void without any loss. Also this better matches the
Linux device model as remove functions are not supposed to fail.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20230512173810.131447-3-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
It is preferred to use typed property access functions (i.e.
of_property_read_<type> functions) rather than low-level
of_get_property/of_find_property functions for reading properties.
Convert reading boolean properties to to of_property_read_bool().
Signed-off-by: Rob Herring <robh@kernel.org>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20230310144727.1545699-1-robh@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
It is preferred to use typed property access functions (i.e.
of_property_read_<type> functions) rather than low-level
of_get_property/of_find_property functions for reading properties. As
part of this, convert of_get_property/of_find_property calls to the
recently added of_property_present() helper when we just want to test
for presence of a property and nothing more.
Signed-off-by: Rob Herring <robh@kernel.org>
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20230310144727.1545630-1-robh@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There is no point in casting a struct uart_port to a struct imx_port
just to access the first member of the latter (a struct uart_port).
This introduces no code changes.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20230302115417.1860210-1-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
cpp_check reports
drivers/tty/serial/imx.c:1207:15: style: Condition 'r_bytes>0' is always true [knownConditionTrueFalse]
if (r_bytes > 0) {
r_byte is set to
r_bytes = rx_ring->head - rx_ring->tail;
The head - tail calculation is also done by the earlier check
if (rx_ring->head <= sg_dma_len(sgl) &&
rx_ring->head > rx_ring->tail) {
so r_bytes will always be > 0, so the second check is not needed.
Signed-off-by: Tom Rix <trix@redhat.com>
Reviewed-by: Iuliana Prodan <iuliana.prodan@nxp.com>
Link: https://lore.kernel.org/r/20230211154550.2130670-1-trix@redhat.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Neither registers shadowing is functionally needed as all the registers are
read-write, nor the shadowing makes much sense for speed-up, as most speed
critical reads/writes (of data Rx/Tx registers) are not shadowed anyway.
Moreover, the shadowing code is obviously pure overhead on the write path.
Get rid of the shadowing code and variables due to above considerations.
Signed-off-by: Sergey Organov <sorganov@gmail.com>
Link: https://lore.kernel.org/r/20230201141603.4205-1-sorganov@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The 'rx' is chip register, similar to 'usr2', so let it be of 'u32' type as
well.
Move 'flg' to be FIFO read loop local as it's not used outside.
Signed-off-by: Sergey Organov <sorganov@gmail.com>
Link: https://lore.kernel.org/r/20230201142700.4346-8-sorganov@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The chip provides all the needed bits in the URXD0 register that we read
anyway for data, so get rid of reading USR2 and use only URXD0 bits
instead.
Signed-off-by: Sergey Organov <sorganov@gmail.com>
Link: https://lore.kernel.org/r/20230201142700.4346-7-sorganov@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There is no need to read USR2 twice at every loop iteration: get rid of the
second read.
Signed-off-by: Sergey Organov <sorganov@gmail.com>
Link: https://lore.kernel.org/r/20230201142700.4346-6-sorganov@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There is no reason to prematurely break out of FIFO reading loop, and it
might cause needless reenters into ISR, so keep reading until FIFO is
empty.
Signed-off-by: Sergey Organov <sorganov@gmail.com>
Link: https://lore.kernel.org/r/20230201142700.4346-5-sorganov@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Do not call uart_handle_sysrq_char() if we got any receive error along with
the character, as we don't want random junk to be considered a sysrq.
Signed-off-by: Sergey Organov <sorganov@gmail.com>
Link: https://lore.kernel.org/r/20230201142700.4346-4-sorganov@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Check if hardware Rx flood is in progress, and issue soft reset to UART to
stop the flood.
A way to reproduce the flood (checked on iMX6SX) is: open iMX UART at 9600
8N1, and from external source send 0xf0 char at 115200 8N1. In about 90% of
cases this starts a flood of "receiving" of 0xff characters by the iMX UART
that is terminated by any activity on RxD line, or could be stopped by
issuing soft reset to the UART (just stop/start of RX does not help). Note
that in essence what we did here is sending isolated start bit about 2.4
times shorter than it is to be if issued on the UART configured baud rate.
There was earlier attempt to fix similar issue in: 'commit
b38cb7d25711 ("serial: imx: Disable new features of autobaud detection")',
but apparently it only gets harder to reproduce the issue after that
commit.
Signed-off-by: Sergey Organov <sorganov@gmail.com>
Link: https://lore.kernel.org/r/20230201142700.4346-3-sorganov@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
We perform soft reset in 2 places, slightly differently for no sufficient
reasons, so move more generic variant to a function, and re-use the code.
Out of 2 repeat counters, 10 and 100, select 10, as the code works at
interrupts disabled, and in practice the reset happens immediately.
Signed-off-by: Sergey Organov <sorganov@gmail.com>
Link: https://lore.kernel.org/r/20230201142700.4346-2-sorganov@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There maybe pending USR interrupt before requesting irq, however
uart_add_one_port has not executed, so there will be kernel panic:
[ 0.795668] Unable to handle kernel NULL pointer dereference at virtual addre
ss 0000000000000080
[ 0.802701] Mem abort info:
[ 0.805367] ESR = 0x0000000096000004
[ 0.808950] EC = 0x25: DABT (current EL), IL = 32 bits
[ 0.814033] SET = 0, FnV = 0
[ 0.816950] EA = 0, S1PTW = 0
[ 0.819950] FSC = 0x04: level 0 translation fault
[ 0.824617] Data abort info:
[ 0.827367] ISV = 0, ISS = 0x00000004
[ 0.831033] CM = 0, WnR = 0
[ 0.833866] [0000000000000080] user address but active_mm is swapper
[ 0.839951] Internal error: Oops: 0000000096000004 [#1] PREEMPT SMP
[ 0.845953] Modules linked in:
[ 0.848869] CPU: 0 PID: 1 Comm: swapper/0 Not tainted 6.1.1+g56321e101aca #1
[ 0.855617] Hardware name: Freescale i.MX8MP EVK (DT)
[ 0.860452] pstate: 000000c5 (nzcv daIF -PAN -UAO -TCO -DIT -SSBS BTYPE=--)
[ 0.867117] pc : __imx_uart_rxint.constprop.0+0x11c/0x2c0
[ 0.872283] lr : imx_uart_int+0xf8/0x1ec
The issue only happends in the inmate linux when Jailhouse hypervisor
enabled. The test procedure is:
while true; do
jailhouse enable imx8mp.cell
jailhouse cell linux xxxx
sleep 10
jailhouse cell destroy 1
jailhouse disable
sleep 5
done
And during the upper test, press keys to the 2nd linux console.
When `jailhouse cell destroy 1`, the 2nd linux has no chance to put
the uart to a quiese state, so USR1/2 may has pending interrupts. Then
when `jailhosue cell linux xx` to start 2nd linux again, the issue
trigger.
In order to disable irqs before requesting them, both UCR1 and UCR2 irqs
should be disabled, so here fix that, disable the Ageing Timer interrupt
in UCR2 as UCR1 does.
Fixes: 8a61f0c70ae6 ("serial: imx: Disable irqs before requesting them")
Suggested-by: Sherry Sun <sherry.sun@nxp.com>
Reviewed-by: Sherry Sun <sherry.sun@nxp.com>
Signed-off-by: Peng Fan <peng.fan@nxp.com>
Acked-by: Jason Liu <jason.hui.liu@nxp.com>
Link: https://lore.kernel.org/r/20230206013016.29352-1-sherry.sun@nxp.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Convert uart_handle_cts_change() to bool which is more appropriate
than unsigned int.
Rename status to active to better describe what the parameter means.
While at it, make the comment about the active parameter easier to
parse.
Cleanup callsites from operations that are not necessary with bool.
Reviewed-by: Jiri Slaby <jirislaby@kernel.org>
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20230117090358.4796-10-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
If a RX_DURING_TX GPIO is defined by the DT property "rs485-rx-during-tx-gpios"
this patch switches this GPIO accordingly to the RS485 flag RX_DURING_TX in user
space. In addition, the i.MX UART receiver is no longer turned on and off during
sending, because now the hardware is responsible for connecting or disconnecting
RX during TX controlled by this GPIO.
Signed-off-by: Christoph Niedermaier <cniedermaier@dh-electronics.com>
Link: https://lore.kernel.org/r/20221202104127.122761-3-cniedermaier@dh-electronics.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The comment in imx_uart_shutdown() says to disable the break condition,
but it doesn't actually do that, here fix this by disabling UCR1_SNDBRK
when closing the uart port like other uart drivers do.
Signed-off-by: Sherry Sun <sherry.sun@nxp.com>
Link: https://lore.kernel.org/r/20221214031137.28815-4-sherry.sun@nxp.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The default polarity of RS485 DE signal is active high. This driver does
not handle such case properly. Currently, when a pin is multiplexed as a
UART CTS_B on boot, this pin is pulled HIGH by the i.MX UART CTS circuit,
which activates DE signal on the RS485 transceiver and thus behave as if
the RS485 was transmitting data, so the system blocks the RS485 bus when
it starts and until user application takes over. This behavior is not OK.
The problem consists of two separate parts.
First, the i.MX UART IP requires UCR1 UARTEN and UCR2 RXEN to be set for
UCR2 CTSC and CTS bits to have any effect. The UCR2 CTSC bit permits the
driver to set CTS (RTS_B or RS485 DE signal) to either level sychronous
to the internal UART IP clock. Compared to other options, like GPIO CTS
control, this has the benefit of being synchronous to the UART IP clock
and thus without glitches or bus delays. The reason for the CTS design
is likely because when the Receiver is disabled, the UART IP can never
indicate that it is ready to receive data by assering CTS signal, so
the CTS is always pulled HIGH by default.
When the port is closed by user space, imx_uart_stop_rx() clears UCR2
RXEN bit, and imx_uart_shutdown() clears UCR1 UARTEN bit. This disables
UART Receiver and UART itself, and forces CTS signal HIGH, which leads
to the RS485 bus being blocked because RS485 DE is incorrectly active.
The proposed solution for this problem is to keep the Receiver running
even after the port is closed, but in loopback mode. This disconnects
the RX FIFO input from the RXD external signal, and since UCR2 TXEN is
cleared, the UART Transmitter is disabled, so nothing can feed data in
the RX FIFO. Because the Receiver is still enabled, the UCR2 CTSC and
CTS bits still have effect and the CTS (RS485 DE) control is retained.
Note that in case of RS485 DE signal active low, there is no problem and
no special handling is necessary. The CTS signal defaults to HIGH, thus
the RS485 is by default set to Receive and the bus is not blocked.
Note that while there is the possibility to control CTS using GPIO with
either CTS polarity, this has the downside of not being synchronous to
the UART IP clock and thus glitchy and susceptible to slow DE switching.
Second, on boot, before the UART driver probe callback is called, the
driver core triggers pinctrl_init_done() and configures the IOMUXC to
default state. At this point, UCR1 UARTEN and UCR2 RXEN are both still
cleared, but UART CTS_B (RS485 DE) is configured as CTS function, thus
the RTS signal is pulled HIGH by the UART IP CTS circuit.
One part of the solution here is to enable UCR1 UARTEN and UCR2 RXEN and
UTS loopback in this driver probe callback, thus unblocking the CTSC and
CTS control early on. But this is still too late, since the pin control
is already configured and CTS has been pulled HIGH for a short period
of time.
When Linux kernel boots and this driver is bound, the pin control is set
to special "init" state if the state is available, and driver can switch
the "default" state afterward when ready. This state can be used to set
the CTS line as a GPIO in DT temporarily, and a GPIO hog can force such
GPIO to LOW, thus keeping the RS485 DE line LOW early on boot. Once the
driver takes over and UCR1 UARTEN and UCR2 RXEN and UTS loopback are all
enabled, the driver can switch to "default" pin control state and control
the CTS line as function instead. DT binding example is below:
"
&gpio6 {
rts-init-hog {
gpio-hog;
gpios = <5 0>;
output-low;
line-name = "rs485-de";
};
};
&uart5 { /* DHCOM UART2 */
pinctrl-0 = <&pinctrl_uart5>;
pinctrl-1 = <&pinctrl_uart5_init>;
pinctrl-names = "default", "init";
...
};
pinctrl_uart5_init: uart5-init-grp {
fsl,pins = <
...
MX6QDL_PAD_CSI0_DAT19__GPIO6_IO05 0x30b1
>;
};
pinctrl_uart5: uart5-grp {
fsl,pins = <
...
MX6QDL_PAD_CSI0_DAT19__UART5_CTS_B 0x30b1
>;
};
"
Tested-by: Christoph Niedermaier <cniedermaier@dh-electronics.com>
Reviewed-by: Fabio Estevam <festevam@denx.de>
Signed-off-by: Marek Vasut <marex@denx.de>
Link: https://lore.kernel.org/r/20220929144400.13571-1-marex@denx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Take advantage of the new uart_xmit_advance() helper.
Reviewed-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-18-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When a UART port is newly registered, uart_configure_port() seeks to
deassert RS485 Transmit Enable by setting the RTS bit in port->mctrl.
However a number of UART drivers interpret a set RTS bit as *assertion*
instead of deassertion: Affected drivers include those using
serial8250_em485_config() (except 8250_bcm2835aux.c) and some using
mctrl_gpio (e.g. imx.c).
Since the interpretation of the RTS bit is driver-specific, it is not
suitable as a means to centrally deassert Transmit Enable in the serial
core. Instead, the serial core must call on drivers to deassert it in
their driver-specific way. One way to achieve that is to call
->rs485_config(). It implicitly deasserts Transmit Enable.
So amend uart_configure_port() and uart_resume_port() to invoke
uart_rs485_config(). That allows removing calls to uart_rs485_config()
from drivers' ->probe() hooks and declaring the function static.
Skip any invocation of ->set_mctrl() if RS485 is enabled. RS485 has no
hardware flow control, so the modem control lines are irrelevant and
need not be touched. When leaving RS485 mode, reset the modem control
lines to the state stored in port->mctrl. That way, UARTs which are
muxed between RS485 and RS232 transceivers drive the lines correctly
when switched to RS232. (serial8250_do_startup() historically raises
the OUT1 modem signal because otherwise interrupts are not signaled on
ancient PC UARTs, but I believe that no longer applies to modern,
RS485-capable UARTs and is thus safe to be skipped.)
imx.c modifies port->mctrl whenever Transmit Enable is asserted and
deasserted. Stop it from doing that so port->mctrl reflects the RS232
line state.
8250_omap.c deasserts Transmit Enable on ->runtime_resume() by calling
->set_mctrl(). Because that is now a no-op in RS485 mode, amend the
function to call serial8250_em485_stop_tx().
fsl_lpuart.c retrieves and applies the RS485 device tree properties
after registering the UART port. Because applying now happens on
registration in uart_configure_port(), move retrieval of the properties
ahead of uart_add_one_port().
Link: https://lore.kernel.org/all/20220329085050.311408-1-matthias.schiffer@ew.tq-group.com/
Link: https://lore.kernel.org/all/8f538a8903795f22f9acc94a9a31b03c9c4ccacb.camel@ginzinger.com/
Fixes: d3b3404df318 ("serial: Fix incorrect rs485 polarity on uart open")
Cc: stable@vger.kernel.org # v4.14+
Reported-by: Matthias Schiffer <matthias.schiffer@ew.tq-group.com>
Reported-by: Roosen Henri <Henri.Roosen@ginzinger.com>
Tested-by: Matthias Schiffer <matthias.schiffer@ew.tq-group.com>
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Signed-off-by: Lukas Wunner <lukas@wunner.de>
Link: https://lore.kernel.org/r/2de36eba3fbe11278d5002e4e501afe0ceaca039.1663863805.git.lukas@wunner.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There should be no reason to adjust old ktermios which is going to get
discarded anyway.
Reviewed-by: Andy Shevchenko <andy.shevchenko@gmail.com>
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220816115739.10928-7-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Embed rs485_supported to uart_port to allow serial core to tweak it as
needed.
Reviewed-by: Lino Sanfilippo <l.sanfilippo@kunbus.com>
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220704094515.6831-2-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
To be able to alter ADDRB within ->rs485_config(), take termios_rwsem
before calling ->rs485_config() and pass termios.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220624204210.11112-5-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The driver provides different rs485_supported for the case where RTS is
not available making it unnecessary to handle it in
imx_uart_rs485_config.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220606100433.13793-32-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add information on supported serial_rs485 features.
In the case where RTS is lacking, RS485 cannot be enabled so provide
zero rs485_supported for that case. Perhaps it would make sense to not
provide rs485_config() at all in that case but such a change would have
userspace visible impact/change in behavior so this patch does not
attempt it.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220606100433.13793-17-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
A few serial drivers make a call to rs485_config() themselves (all
these seem to relate to init). Convert them all to use a common helper
which makes it easy to make adjustments on tasks related to it as
serial_rs485 struct sanitization is going to be added.
In pci_fintek_setup() (in 8250_pci.c), the rs485_config() call was made
with NULL, however, it can be changed to pass uart_port's rs485 struct.
No other callers should pass NULL into rs485_config() so the NULL check
can now be eliminated.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220606100433.13793-2-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Here is the big set of tty and serial driver updates for 5.19-rc1.
Lots of tiny cleanups in here, the major stuff is:
- termbit cleanups and unification by Ilpo. A much needed
change that goes a long way to making things simpler for all
of the different arches
- tty documentation cleanups and movements to their own place in
the documentation tree
- old tty driver cleanups and fixes from Jiri to bring some
existing drivers into the modern world
- RS485 cleanups and unifications to make it easier for
individual drivers to support this mode instead of having to
duplicate logic in each driver
- Lots of 8250 driver updates and additions
- new device id additions
- n_gsm continued fixes and cleanups
- other minor serial driver updates and cleanups
All of these have been in linux-next for weeks with no reported issues.
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Merge tag 'tty-5.19-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty
Pull tty and serial driver updates from Greg KH:
"Here is the big set of tty and serial driver updates for 5.19-rc1.
Lots of tiny cleanups in here, the major stuff is:
- termbit cleanups and unification by Ilpo. A much needed change that
goes a long way to making things simpler for all of the different
arches
- tty documentation cleanups and movements to their own place in the
documentation tree
- old tty driver cleanups and fixes from Jiri to bring some existing
drivers into the modern world
- RS485 cleanups and unifications to make it easier for individual
drivers to support this mode instead of having to duplicate logic
in each driver
- Lots of 8250 driver updates and additions
- new device id additions
- n_gsm continued fixes and cleanups
- other minor serial driver updates and cleanups
All of these have been in linux-next for weeks with no reported issues"
* tag 'tty-5.19-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty: (166 commits)
tty: Rework receive flow control char logic
pcmcia: synclink_cs: Don't allow CS5-6
serial: stm32-usart: Correct CSIZE, bits, and parity
serial: st-asc: Sanitize CSIZE and correct PARENB for CS7
serial: sifive: Sanitize CSIZE and c_iflag
serial: sh-sci: Don't allow CS5-6
serial: txx9: Don't allow CS5-6
serial: rda-uart: Don't allow CS5-6
serial: digicolor-usart: Don't allow CS5-6
serial: uartlite: Fix BRKINT clearing
serial: cpm_uart: Fix build error without CONFIG_SERIAL_CPM_CONSOLE
serial: core: Do stop_rx in suspend path for console if console_suspend is disabled
tty: serial: qcom-geni-serial: Remove uart frequency table. Instead, find suitable frequency with call to clk_round_rate.
dt-bindings: serial: renesas,em-uart: Add RZ/V2M clock to access the registers
serial: 8250_fintek: Check SER_RS485_RTS_* only with RS485
Revert "serial: 8250_mtk: Make sure to select the right FEATURE_SEL"
serial: msm_serial: disable interrupts in __msm_console_write()
serial: meson: acquire port->lock in startup()
serial: 8250_dw: Use dev_err_probe()
serial: 8250_dw: Use devm_add_action_or_reset()
...
Not much dramatic changes at this time, but we've received quite
a lot of changes for ASoC, while there are still a few fixes and
quirks for usual HD- and USB-auido. Here are some highlights.
* ASoC:
- Overhaul of endianness specification for data formats, avoiding
needless restrictions due to CODECs
- Initial stages of Intel AVS driver merge
- Introduction of v4 IPC mechanism for SOF
- TDM mode support for AK4613
- Support for Analog Devices ADAU1361, Cirrus Logic CS35L45, Maxim
MAX98396, MediaTek MT8186, NXP i.MX8 micfil and SAI interfaces,
nVidia Tegra186 ASRC, and Texas Instruments TAS2764 and TAS2780
* Others
- A few regression fixes after the USB-audio endpoint management
refactoring
- More enhancements for Cirrus HD-audio codec support (still ongoing)
- Addition of generic serial MIDI driver
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Merge tag 'sound-5.19-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/tiwai/sound
Pull sound updates from Takashi Iwai:
"Not much dramatic changes at this time, but we've received quite a lot
of changes for ASoC, while there are still a few fixes and quirks for
usual HD- and USB-auido. Here are some highlights.
ASoC:
- Overhaul of endianness specification for data formats, avoiding
needless restrictions due to CODECs
- Initial stages of Intel AVS driver merge
- Introduction of v4 IPC mechanism for SOF
- TDM mode support for AK4613
- Support for Analog Devices ADAU1361, Cirrus Logic CS35L45, Maxim
MAX98396, MediaTek MT8186, NXP i.MX8 micfil and SAI interfaces,
nVidia Tegra186 ASRC, and Texas Instruments TAS2764 and TAS2780
Others:
- A few regression fixes after the USB-audio endpoint management
refactoring
- More enhancements for Cirrus HD-audio codec support (still ongoing)
- Addition of generic serial MIDI driver"
* tag 'sound-5.19-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/tiwai/sound: (504 commits)
ALSA: hda/realtek - Add new type for ALC245
ALSA: usb-audio: Configure sync endpoints before data
ALSA: ctxfi: fix typo in comment
ALSA: cs5535audio: fix typo in comment
ALSA: ctxfi: Add SB046x PCI ID
ALSA: usb-audio: Add missing ep_idx in fixed EP quirks
ALSA: usb-audio: Workaround for clock setup on TEAC devices
ALSA: lola: Bounds check loop iterator against streams array size
ASoC: max98090: Move check for invalid values before casting in max98090_put_enab_tlv()
ASoC: rt1308-sdw: add the default value of register 0xc320
ASoC: rt9120: Use pm_runtime and regcache to optimize 'pwdnn' logic
ASoC: rt9120: Fix 3byte read, valule offset typo
ASoC: amd: acp: Set Speaker enable/disable pin through rt1019 codec driver.
ASoC: amd: acp: Set Speaker enable/disable pin through rt1019 codec driver
ASoC: wm2000: fix missing clk_disable_unprepare() on error in wm2000_anc_transition()
ASoC: codecs: lpass: Fix passing zero to 'PTR_ERR'
ASoC: SOF: sof-client-ipc-flood-test: use pm_runtime_resume_and_get()
ASoC: SOF: mediatek: remove duplicate include in mt8195.c
ASoC: SOF: mediatek: Add mt8195 debug dump
ASoC: SOF: mediatek: Add mediatek common debug dump
...
The i.MX DMA drivers are device tree only, nothing in
include/linux/platform_data/dma-imx.h has platform_data in it, so move
the file to include/linux/dma/imx-dma.h.
Signed-off-by: Sascha Hauer <s.hauer@pengutronix.de>
Acked-By: Vinod Koul <vkoul@kernel.org>
Link: https://lore.kernel.org/r/20220414162249.3934543-10-s.hauer@pengutronix.de
Signed-off-by: Mark Brown <broonie@kernel.org>
Commit 76821e222c18 ("serial: imx: ensure that RX irqs are off if RX is
off") accidentally enabled overrun interrupts unconditionally when
deferring DMA enable until after the receiver has been enabled during
startup.
Fix this by using the DMA-initialised instead of DMA-enabled flag to
determine whether overrun interrupts should be enabled.
Note that overrun interrupts are already accounted for in
imx_uart_clear_rx_errors() when using DMA since commit 41d98b5da92f
("serial: imx-serial - update RX error counters when DMA is used").
Fixes: 76821e222c18 ("serial: imx: ensure that RX irqs are off if RX is off")
Cc: stable@vger.kernel.org # 4.17
Cc: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Johan Hovold <johan@kernel.org>
Link: https://lore.kernel.org/r/20220411081957.7846-1-johan@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In uart_set_rs485_config() the serial core already assigns the passed
serial_rs485 struct to the uart port.
So remove the assignment in the drivers rs485_config() function to avoid
reduncancy.
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Lino Sanfilippo <LinoSanfilippo@gmx.de>
Link: https://lore.kernel.org/r/20220410104642.32195-8-LinoSanfilippo@gmx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Currently, uart_console_write->putchar's second parameter (the
character) is of type int. It makes little sense, provided uart_console_write()
accepts the input string as "const char *s" and passes its content -- the
characters -- to putchar(). So switch the character's type to unsigned
char.
We don't use char as that is signed on some platforms. That would cause
troubles for drivers which (implicitly) cast the char to u16 when
writing to the device. Sign extension would happen in that case and the
value written would be completely different to the provided char. DZ is
an example of such a driver -- on MIPS, it uses u16 for dz_out in
dz_console_putchar().
Note we do the char -> uchar conversion implicitly in
uart_console_write(). Provided we do not change size of the data type,
sign extension does not happen there, so the problem is void.
This makes the types consistent and unified with the rest of the uart
layer, which uses unsigned char in most places already. One exception is
xmit_buf, but that is going to be converted later.
Cc: Paul Cercueil <paul@crapouillou.net>
Cc: Tobias Klauser <tklauser@distanz.ch>
Cc: Russell King <linux@armlinux.org.uk>
Cc: Vineet Gupta <vgupta@kernel.org>
Cc: Nicolas Ferre <nicolas.ferre@microchip.com>
Cc: Alexandre Belloni <alexandre.belloni@bootlin.com>
Cc: Ludovic Desroches <ludovic.desroches@microchip.com>
Cc: Florian Fainelli <f.fainelli@gmail.com>
Cc: bcm-kernel-feedback-list@broadcom.com
Cc: Alexander Shiyan <shc_work@mail.ru>
Cc: Baruch Siach <baruch@tkos.co.il>
Cc: "Maciej W. Rozycki" <macro@orcam.me.uk>
Cc: Paul Walmsley <paul.walmsley@sifive.com>
Cc: Palmer Dabbelt <palmer@dabbelt.com>
Cc: Albert Ou <aou@eecs.berkeley.edu>
Cc: Shawn Guo <shawnguo@kernel.org>
Cc: Sascha Hauer <s.hauer@pengutronix.de>
Cc: Pengutronix Kernel Team <kernel@pengutronix.de>
Cc: Fabio Estevam <festevam@gmail.com>
Cc: NXP Linux Team <linux-imx@nxp.com>
Cc: Karol Gugala <kgugala@antmicro.com>
Cc: Mateusz Holenko <mholenko@antmicro.com>
Cc: Vladimir Zapolskiy <vz@mleia.com>
Cc: Neil Armstrong <narmstrong@baylibre.com>
Cc: Kevin Hilman <khilman@baylibre.com>
Cc: Jerome Brunet <jbrunet@baylibre.com>
Cc: Martin Blumenstingl <martin.blumenstingl@googlemail.com>
Cc: Taichi Sugaya <sugaya.taichi@socionext.com>
Cc: Takao Orito <orito.takao@socionext.com>
Cc: Liviu Dudau <liviu.dudau@arm.com>
Cc: Sudeep Holla <sudeep.holla@arm.com>
Cc: Lorenzo Pieralisi <lorenzo.pieralisi@arm.com>
Cc: "Andreas Färber" <afaerber@suse.de>
Cc: Manivannan Sadhasivam <mani@kernel.org>
Cc: Michael Ellerman <mpe@ellerman.id.au>
Cc: Benjamin Herrenschmidt <benh@kernel.crashing.org>
Cc: Paul Mackerras <paulus@samba.org>
Cc: Andy Gross <agross@kernel.org>
Cc: Bjorn Andersson <bjorn.andersson@linaro.org>
Cc: Krzysztof Kozlowski <krzysztof.kozlowski@canonical.com>
Cc: Orson Zhai <orsonzhai@gmail.com>
Cc: Baolin Wang <baolin.wang7@gmail.com>
Cc: Chunyan Zhang <zhang.lyra@gmail.com>
Cc: Patrice Chotard <patrice.chotard@foss.st.com>
Cc: Maxime Coquelin <mcoquelin.stm32@gmail.com>
Cc: Alexandre Torgue <alexandre.torgue@foss.st.com>
Cc: "David S. Miller" <davem@davemloft.net>
Cc: Peter Korsgaard <peter@korsgaard.com>
Cc: Michal Simek <michal.simek@xilinx.com>
Acked-by: Richard Genoud <richard.genoud@gmail.com> [atmel_serial]
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Acked-by: Paul Cercueil <paul@crapouillou.net>
Acked-by: Neil Armstrong <narmstrong@baylibre.com> # meson_serial
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Link: https://lore.kernel.org/r/20220303080831.21783-1-jslaby@suse.cz
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Right now, even when `delay_rts_before_send` and `delay_rts_after_send`
are 0, the hrtimer is triggered (with timeout 0) which can introduce a
few 100us of additional overhead on slower i.MX platforms.
Implement a fast path when the delays are 0, where the RTS signal is
toggled immediately instead of going through an hrtimer. This fast path
behaves identical to the code before delay support was implemented.
Reviewed-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Harald Seiler <hws@denx.de>
Link: https://lore.kernel.org/r/20220119145204.238767-1-hws@denx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Triggering RX interrupt for every byte defeats the purpose of aging
timer and leads to interrupt storm at high baud rates. The interrupt
storm can starve line discipline worker and prevent tty throttling,
rendering hardware/software flow control useless.
Increase receiver trigger level to 8 to increase the minimum period
between RX interrupts to 8 characters time. The tradeoff is increased
latency.
Aging timer resets with every received character. Worst case scenario
happens when RX data intercharacter delay is slightly less than the
aging timer timeout (8 characters time). The upper bound of the time
a character can wait in RxFIFO before interrupt is raised is:
(RXTL - 1) * (8 character time timeout + received 1 character time)
Usually the data is received in frames, with low intercharacter delay.
In such case the latency increase is 8 characters time at the end of
the frame with probability (RXTL - 1) / RXTL.
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Tomasz Moń <tomasz.mon@camlingroup.com>
Link: https://lore.kernel.org/r/20220117060417.624613-1-tomasz.mon@camlingroup.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The UCR4_OREN should be disabled before disabling the uart receiver in
.stop_rx() instead of in the .shutdown().
Otherwise, if we have the overrun error during the receiver disable
process, the overrun interrupt will keep trigging until we disable the
OREN interrupt in the .shutdown(), because the ORE status can only be
cleared when read the rx FIFO or reset the controller. Although the
called time between the receiver disable and OREN disable in .shutdown()
is very short, there is still the risk of endless interrupt during this
short period of time. So here change to disable OREN before the receiver
been disabled in .stop_rx().
Signed-off-by: Fugang Duan <fugang.duan@nxp.com>
Signed-off-by: Sherry Sun <sherry.sun@nxp.com>
Link: https://lore.kernel.org/r/20211125020349.4980-1-sherry.sun@nxp.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Clear RTSD status before enabling the irq event for RTSD in
imx_uart_enable_wakeup function.
Since RTSD can be set as the wakeup source, this can avoid any risk of
false triggering of a wake-up interrupts.
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Fugang Duan <fugang.duan@nxp.com>
Signed-off-by: Sherry Sun <sherry.sun@nxp.com>
Link: https://lore.kernel.org/r/20211125014306.4432-1-sherry.sun@nxp.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
During console setup imx_uart_console_setup() enables clocks, but they
are never disabled when the console is unregistered, this leads to
clk_prepare_enable() being called multiple times without a matching
clk_disable_unprepare() in case of console unregister.
Ensure that clock enable/disable are balanced adding
clk_disable_unprepare() in the console exit callback.
Signed-off-by: Francesco Dolcini <francesco.dolcini@toradex.com>
Link: https://lore.kernel.org/r/20211020192643.476895-3-francesco.dolcini@toradex.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In order to optimize serial communication (performance/throughput VS
latency), we may need to tweak DMA period number and size. This adds
DT properties to configure those values before initialising DMA.
The defaults will stay the same as before.
[update documentation and commit message, rebase to current master,
switch back to DT instead of sysfs]
Signed-off-by: Fabien Lahoudere <fabien.lahoudere@collabora.com>
Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.com>
Link: https://lore.kernel.org/r/20210430175038.103226-2-sebastian.reichel@collabora.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There's no need to initialise irq-flags variables before saving the
interrupt state.
Drop the redundant initialisations from drivers that got this wrong.
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Johan Hovold <johan@kernel.org>
Link: https://lore.kernel.org/r/20210519092541.10137-1-johan@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Force-threaded interrupt handlers used to run with interrupts enabled,
something which could lead to deadlocks in case a threaded handler
shared a lock with code running in hard interrupt context (e.g. timer
callbacks) and did not explicitly disable interrupts.
This was specifically the case for serial drivers that take the port
lock in their console write path as printk can be called from hard
interrupt context also with forced threading ("threadirqs").
Since commit 81e2073c175b ("genirq: Disable interrupts for force
threaded handlers") interrupt handlers always run with interrupts
disabled on non-RT so that drivers no longer need to do handle this.
Drop the now obsolete workaround added by commit 33f16855dcb9 ("tty:
serial: imx: fix potential deadlock").
Cc: Sam Nobs <samuel.nobs@taitradio.com>
Cc: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Cc: Thomas Gleixner <tglx@linutronix.de>
Cc: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Cc: Peter Zijlstra <peterz@infradead.org>
Signed-off-by: Johan Hovold <johan@kernel.org>
Link: https://lore.kernel.org/r/20210322111036.31966-1-johan@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This really eliminates multiplications from the assembly. I would have
thought they are optimized by inlining ktime_set, but not on x86_64 with
gcc 10.
Cc: Shawn Guo <shawnguo@kernel.org>
Cc: Sascha Hauer <s.hauer@pengutronix.de>
Cc: Pengutronix Kernel Team <kernel@pengutronix.de>
Cc: Fabio Estevam <festevam@gmail.com>
Cc: NXP Linux Team <linux-imx@nxp.com>
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Link: https://lore.kernel.org/r/20210302062214.29627-10-jslaby@suse.cz
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>